Hello all,
I am working on getting my robot up and running and did the limit switch test and all the limit switches are in the high state in the normal position and low state when the switch is activated. Reviewed all wiring and can’t find any issues. Does any one have some advice on why this is or a solution.
Thanks
Yes that is exactly what I did. I flip flopped the 2 on accident. Took me a few times looking at it to realize. Thanks for the help